Rick Lucas: Ping
I was convinced that the table/pole link was
sufficient to hold the table in place so I turned my efforts toward the two
mounts at the top and bottom. The teak that was used at the top was very well
honed and looked very nice, but the two screws that were originally used to
affix the pole to the base were splitting the wood and pulling it apart. The two
pieces of wood that made up the assembly were also not securely fixed to one
another, allowing the one with the pole attached to it to shift around inside
the larger piece. Those two issues needed to be resolve.
The other solution is where the cosmetic aspects
of the solution get really dodgy. The screws that went through the wood and into
the pole would cause the wood to split when lateral pressure was applied. I
didn't think that glue would be enough to put this Humpty Dumpty back together
for the long term because the wood grain ran vertically, from the top of the
piece to the bottom. Fixing one split would only invite another.
A hose clamp was the best thing I could come up
with to keep the wood from splitting and providing a solid surface that would
keep the screws and the pole in place. I first put glue on the split wood on the
inside, where the pole would go. I then tightened the hose clamp around the wood
and slid the complete wooden base over the pole. I then drilled two holes in the
hose clamp in line with the existing ones in the wood base. Next, back went the
screws into the holes to hold it to the pole, and I screwed the whole mess back
into the cabin roof. Once all the glue had cured, I gave the table the pressure
test. Success! The two screws held the pole to the teak bracket and the table
didn't move... much.
(UPDATE: I removed the cap and epoxied the two
pieces of wood together. There was enough room above the level of the tube to
add some glass fabric for added strength. I also replaced the two screws and
clamp with long, thin bolts that go all the way through. It turns out that with
the brackets on the foot of the tube [described below], the clamp was no longer
needed.)
I did notice that the bottom
of the pole would still move around a little when I moved the table. Some kind
of angle brackets seemed to be the answer. I couldn't find anything suitable at
the local chandlery or at SailNet so I searched until I found some in solid
brass at the local Ace hardware store. I know that brass isn't the strongest
metal, but I didn't want it to take the whole load. I just needed them to
provide additional stability to the bottom of the pole. That it did. While not
perfectly solid, the table's motion is now less than one inch.
Things I'd do differently: Nothing now since I added the epoxy and cloth to the cap. It solved the problem.
Cost: Less than US$10.00 (hardware)
The
design of the settee table on the 323 is not particularly robust. I've heard
stories from other owners about how theirs can swing like a pendulum on a clock.
Not only is this a messy situation. It could be hazardous to anyone below,
especially at dinnertime when four people are sawing on their steaks at the same
time.
For reasons unknown to me,
Ping's PO replaced the support pole and both it's mounting brackets. The new
bottom mount had nothing to keep the pole from turning, and the top mount just
couldn't do the job alone. The table secures to the pole by a round bracket that
exerts pressure on the pole with a knurled screw knob. When a 200 lb. man leans
on the corner of the table without the pole being fully secured, something had
to give. In this case, it was the pole turning in its mounts.
The solution was not the most
elegant I've ever devised, but it was effective. I first unscrewed the wooden
base from the cabin roof and removed it from the pole. I applied some polyester
glue to bond the two pieces of wood together and set the assembly aside to dry.
Polyester glue works wonderfully well on wood and other substances, but it has a
tendency to expand and bubble out from the gaps as it dries. The bubbles can be
easily removed within 24 hours of application, but after it has fully cured you
may as well try to separate the minstrel from Jimmy Buffett! The tan residue you
see in the picture at left is the part of that overflow that I couldn't remove a
week after I applied the glue. Oh well. If I get motivated, I can probably clean
it up with a Dremel cut wheel.
The solution, at present, is a tradeoff. The
table's stable, but the aesthetics of the installation aren't quite as nice as
they used to be. Since I don't know what was there originally, I don't
have the benefit of the factory installation as a model. So, for now, I'll leave
it as is.
Time: About 3 hours